The #2 aileron servo (port side) had a different range of motion than the #1 pitch servo (starboard side), causing a CCPM interaction at either end other of motion. I could not overcome this with endpoints for some reason, so I decided to replace the servos. I bought some inexpensive digital MG90 micro servos and tonight I installed them. Tomorrow I will program the ZYX Flybarless system and weather permitting test fly her! I will take her and the 450 Sport (flybarred) out.
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