Met up with Kenny at MCRCC, and the crowd thickened as the day went on. Jason was there helping tune up engines, and got both of Kenny's running. Finally his 1/4 scale Cub running well, he enjoyed flying it in the moderate winds. It ran smooth as silk. Still working on his Sbach engine when I left.
The flying monkeys got me...
Monday, May 26, 2014
A nice simple day
Met up with Kenny at MCRCC, and the crowd thickened as the day went on. Jason was there helping tune up engines, and got both of Kenny's running. Finally his 1/4 scale Cub running well, he enjoyed flying it in the moderate winds. It ran smooth as silk. Still working on his Sbach engine when I left.
Saturday, May 24, 2014
Skyline/Goldwing Sbach 70 60" #2 Flight Ready
She has the same power system and electronics. I have a 17x8 prop on her (turns out I had a 17x7 on before). I have ordered a 3 blade 16x8 EMP prop and a Du-Bro plastic 3 blade spinner. These don't come in 2-1/4', so had to get a 2". On a quick power test this morning I got a peak of around 1540 watts. Curious how the 3 blade will perform.
Common to both is that the wrong decals are included in the kit. Instead of the stickers for the red-white-black one, they come with the set common to the other colors. The white letters obviously don't show up on the white wings. General Hobby says they are sending the right ones, but last time even giving me a tracking number didn't get them in the mail so I am not holding my breath. The only one missing, really, is the large Sbach 342 that should be on the top left wing.
All in all, she setup. CG'd and looks identical to the first one. Looking forward to the maiden flight!
Tuesday, May 20, 2014
Don't Give Up!
I also can't stand an unsolved problem, so today, after a couple of days of walking past the bin with agita every time I saw the heli, I pulled it out and worked on isolating the gyro. Nothing really worked well. And then I remembered seeing a drawing on an Align gyro manual that showed various possible positions for the gyro, and I remember one in front of the main shaft rather than the traditional aft of the main shaft. This would move the gyro away from the finely vibrating boom and tail. I also changed the tail blades (weight balanced against one another) and new main blades, I changed the main and feathering shafts, and improved smoothness of movement in the tail assembly. This this is as clean vibration wise as I can possibly make it.
So, in main blades off spin ups the rudder servo was still and not being affected by vibration! I had to modify the canopy to allow the gyro forward. Tomorrow I will try hovering and possibly flying it!
UPDATE-UPDATE: So... I got to thinking, maybe its the Align 780 gyro? I threw an Assan GA250 gyro I had in the box on her and spun her up. She still has a very high freq vibration, but the gyro held and she didn't wag, nor did she shake herself apart! I plan to see what happens at the field on Memorial Day. I did order a $30 Hobby King 450 Pro V2 chassis to replace her though.
Thursday, May 15, 2014
The Cat-Proof Castle, Sbach Mod
That'll do...
Monday, May 12, 2014
The Second Sbach 70 arrived today...
I wonder if I have the skills to create a background in black cote that I could put the sticker on?
Sunday, May 11, 2014
Saturday, May 10, 2014
EXI45 Sport Flight Ready. Again.
I made a few programming changes that I think will have a significant impact. I removed my looney "soft" mode of 80% pitch limits in Idle2 (WTF...) as I realized that this changed the slope of the pitch curve relative to the full 100% pitch range curve in Idle3. This was why I got a little skip switching between idle-ups. Stupid. I kept the novel Idle1 of zero pitch across the board. Now there is no difference between Idle 2 and 3.
I also decided to go back to DR of 50-75-100, and 25% expo across the board. I need the finer expo for control. We'll see how that goes.
Next step, test crashing, I mean, um, test flying.
UPDATE: Spun it up and there is some wacky vibration, fine occasional coarse, low amplitude high velocity, coming from the tail assembly when the blade hub is put on (with or without blades). Happens at certain rpm and pitch. I changed the bearings, blades, tightened up, still there. Its pretty impressive and loosened all the bolts despite liberal locktite. I can't fix it. There is a hint of play in the bearing hub and the tail shaft hence has a touch of play. I decided to just order a Tarot tail assembly...
Monday, May 5, 2014
EXI 450 Rebuild, Billionth Time
So...
The other day I was flying the EXI450 Sport, trying to isolate some severe vibrations that were causing a tail wag, making the gyro gain very impossible to nail down, while also trying to figure out what rates and expo I like, when the tail belt snapped and she instantly pretzeled four feet off the ground onto the pavement. It was one big ball. One main blade sailed over my head (a good 15 feet), and the tail boom snapped off from the torque. The gyro took a blade hit as it flew off its perch and has a nice dent in the case, and the tail blades became shrapnel. The solid steel main rotor shaft bent at 45 degrees, and even the solid block aluminum rotor head got a 2-3 degree tilt in it (can't see it, but when I replaced the shaft there was a significant wobble in the rotor head not present with shaft alone). The tail shaft also got tweaked. Needless to say, the fly bar was a swirly. None of the servos failed, however, all passing inspection and motion testing. There is a tremendous amoun of energy in these helis, and it all instantly traded places.
I was annoyed and damned if once again I didn't fail to take a pic.
Ordered a new tail boom (of course I have hundreds in storage...) and a new Align Sport rotor head block. I didn't expect them so soon but they arrived today! I took apart the entire swash cage and rebuilt it with the new rotor head, cleaning and lubing up everything that moved. New flybar installed, a few mm shorter than the ruined one. While I was waiting for these parts I replaced the main shaft, the stripped main gear. I had also rebuilt the tail assembly. I didn't realize I had built it backwards, even after I installed the tail boom and it had to go in upside down (I even cut a new detente groove in the forward end). I have used Tarot booms which required an upside down installation on an Align machine, and I thought maybe the original tail housing on the frame was a Tarot, so didn't think too much of it. Today after I had reinstalled the tail housing, boom and tail rotor assembly, I realized I forgot to put the control rod guides and the servo clamps on the boom first ... (I was way distracted with an upcoming business trip). I took everything apart again, slid the tail boom pieces on there and rebuilt it. When I went to put the tail guard/vert stabilizer on, I realized I had assembled the tail assembly backwards! That's why the slot was on the wrong side and I installed the boom upside down, dammit. So I had to dis-assemble the tail assembly and re-assmble it properly, pulling it off the boom and drilling the rear pin detente hole on the "wrong" side, and reassembling it. In the end I basically installed the tail boom upside down and had to McGyver the forward and aft tail boom detentea. What a frickin' waste of time, but I didn't want to waste the tail boom. This is so not like me...
It all works fine. Without blades there is very litte fine vibration. I re-installed the tail servo and control rod, but haven't set them in place. I'll do that when I come back. Installed the brace supports and called it a night.
Took this photo during a break, before putting the tail boom braces back on. Next time, balance the new main blades and install them, and the tail blades, set up the tail and fix the tail servo in place, then see if all this cleaning and replacing fixed the vibration issues! This heli has been rebuilt so many times....
Sunday, May 4, 2014
Another death in the family...
It started out well. I went out solo this morning, first on the field and had it all to myself. Virtually no winds, occasionally a brisk crosswind gust, but never threatening. A quiet Sunday morning at MCRCC. I got out there around 10am, ready to go.
I took Aidan's Alpha 450 up, and ran it through its paces. She flew great with her extra nose weight, and I practiced short and cross wind landings as well as work on orientation. She is tight in control, predictable and rugged, everything you want in a trainer. She's a keeper, and I am glad Aidan and I each have one to keep our basic flight skills honed, and to share this hobby with others. I flew a couple of packs, but then that clicking noise came back when she tipped over her feet in the thick grass despite bigger tires. The rotor was on the move again. I tweaked her up and she flew fine. After 4 packs I put her away for the day. That'll do girl, that'll do.
When I got her home I took the prop off and realized there are cut out flat spots on the motor shaft, so I worked to get the lock screw to set in there with some locktite and gorilla snugged it into place. Hope that's the end of it.
After that I took the Pulse up and ran her through some aerobatics, getting mentally in place to follow up those aerobatics on the Sbach. She is so well built and tuned, not a vibration anywhere. her motor ran true and silent. I flew her for one pack, sweet, high powered high altitude work, a couple of touch and goes in the northerly crosswind, and decided I was ready to take the Sbach up.
The Sbach flew like a dream... Sweet smooth effortless takeoff, into some high altitude, high speed, high G, high torque aerobatics. I put her through the wringer. I noticed a final set of loops and Cuban 8's that were less round, a little uncommanded roll as she came around. I swung her hard into a final loop to pull out into final from the south. She took off skyward like the rocket she is, a bit of un commanded roll, I pulled her back into a loop, and realized I wasn't flying her anymore. I tried to correct, no repsonse, then zeroed the controls, nothing. She waffled out of the top of the loop in a slow shuddering spin, powered her off and called out that I had no control. She was high as she came down, twisting, screaming, and slammed into the ground nose first. She hit so hard she bounced up scattering pieces all over, a wing cast off across the runway, and came to a rest in a crumpled heap about 6 feet away from the impact site. No chute, no fire... The pilot was surely dead...
Curiously, neither the prop, motor, electronics, landing gear nor the wings and tail, for the most part, had any significant damage. The fuse was powdered, but that was it.
I wasn't sure what I would do... I recovered all the electronics and they all seem to function well. I ordered a replacement SK3-5055 prop adapter, but am not sure I will replace the plane right now. Surely I will.
UPDATE: I was looking at the HobbyKing version, but after an hour dicking around with their website issues, I learned it would cost an additional $73 to ship their version from the USA warehouse. Great price for the plane, but the shipping killed. Since the General Hobby Skyline version was a good plane really, and on sale for two more days with $25 shipping, still way under the HobbyKing cost, I opted to go ahead and replace it from General Hobby. Since I was leery of the supplied hinges and they failed, I have also ordered nylon and metal hinges from Hobbylinc for cheap. The new plane will have reliable hinges.
When. I come back from a business trip this week all the parts and the plane should be here. Should be a quick build.
Saturday, May 3, 2014
A Very Excellent Day!
Aidan and I headed out this morning for a date on the MCRCC flightline, looking to maiden his Alpha Sport 450 and my PulseXT 25e after a breakfast of southerner at Das House of Waffles. It was a spectacular day!
The Alpha flew tail heavy, which surprised me for two reasons. Firstly, despite telling Aidan we needed to check CG I completely forgot to do it, and secondly, this is not a tail heavy plane. I ended up putting an ounce in the nose. So the first flight was brief and I had to land cross field because I didn't feel like dealing with the cross wind, and at the last minute her upwindish wing tossed up a bit. Rough landing, no damage.
In setting up the weight we pulled a loose solder out from the EC3-EC5 adapter I had made out of an old EC3 battery lead. The solder was about 4 years old... I hadn't brought my soldering torch, and at first thought all was lost, but McGyver Me used the clubhouse electric stove to heat the remaining solder in the bad EC3 pin, and voila, fixed it after a couple of tries. I noticed the motor clicking, but couldn't figure out what was up, it otherwise ran fine. We got the plane up and Aidan got to make a few runs on it before we brought her back in. I still heard the clicking and inspected the motor, pulling on the prop. It was then I noticed the brand new Eflite 450 motor's rotor (the can) was pulling off the stator by a good quarter inch. I didn't have a hex driver small enough to fit it, nor did anyone else on the field, so that ended the flight day for the 450. In the meantime we put the bigger tires on her since the stock ones were tripping her up in the grass.
When I got home I removed the motor (none of it was locktited), reset the back "rotor holder thingy", a wheel lock actually and tightened it with some locktite. I reset the stator and replaced the SAE lock nut with a metric as it was stipped in the frickin' lock hole, which is why it slipped, and snugged it all in with locktite. Put it all back together with locktite and gave her a spin up. Ran great, click was gone, rotor stayed put on the stator. I'm going back out tomorrow wx permitting and will fly her through a proper maiden workout; we'll see if I have prevailed over the wayward stator.
I maidened PulseXT 25e #4 today! She flew perfectely as designed. I wasn't feeling lucky, so I put her away after that first flight, but will fly the snot out of her tomorrow!
Ended the day with a nice flight of the Sbach 70, took her through the first aerobatics I have flown for some time, and she did marvelously. it is a distinct pleasure watching her unlimited vertical at high speed. I landed her after 4 minutes, having flown her on a 6S 3300, and the battery was down to 3.7 per cell... This is disappointing as I was getting 6 minutes to that level on 2 x 3S 2560 in series... Tomorrow I will put a 4000 in her and see what time I get. I think putting her on the ground after 4 minutes will be safe until I get a better feel for the run time. 4 minutes sucks... And I flew most of that at half throttle (at which she still hauls ass). After one flight I was done... Spent too much time farting around with fixing the 450.
Good Guy Jerry Gollot, who taught me how to fly, took Aidan up on his 40 sized nitro trainer. Aidan made several turns, getting a feel for how an airplane flies and turns, learning the nuance of a little elevator in a turn, and a light finger on the sticks. He did pretty darn well and of course I failed to take a pic...
All in all, a very successful day! Looking forward to getting out there very early tomorrow and flying before the winds pick up!