First, the success. I have had problems with the soft metal of the spark plug hole in the cylinder of the RCGF 10cc engines. In the past this required buying a new cylimder head for about $55. This past time I was sure someone made something to fix this sort of thing. What I found was that someone had made an adapter to go from a CM-6to a 1/4-32spark plug, for a huge savings.
The flying monkeys got me...
Friday, September 11, 2020
RCGF10CC Blues
Thursday, September 10, 2020
That Wireless Trainer thingy really works!
Since we were hooking up to deliver it and he lives down the street from the SNHRCC field, we met there. He brought his FIL, Steven Hooski. Since Jon is a newbie, and I have great trainer, AND I wanted to see if I could do Trainer mode on the iX12, AND because I wanted to fly, AND because I knew he would benefit and love doing it, I brought the Alpha Sport 450 and 11 packs out to the field. The last 4 were sketchy for a couple of reasons... more on that in a second.
We spent some time going over airplanes and flight controls, the radio, receivers, etc. And then set up to fly. A few adjustments, this was pretty easy to program. I thought that the wireless Trainer mode took all the settings from the Master, the iX12, but I had to make a couple of sub trim adjustments on the DX8. This took no time at. all.On the first couple of packs I took off and let Jon get the feel for the controls, and he was quick to adapt. He was a natural, showed good insight, understanding, so we discussed take off and on the 3rd pack he took off. I landed and he did it again, getting several cycles in. So I offered to land if he set up the approach. He was doing so well that on final I offered a little advice and suggested he continue to land. He aced it. Suggested he turn around on the runway and take off, fly the pattern and do it again. We had him fly the last 3 packs all by himself with my finger on the Trainer button. We chatted, but no advice required nor given, he did it all himself! He seemed pretty excited and really enjoyed it!
I flew one pack when I gave him a break, taking the Hacker MX2 up. After he was done flying, I planned to fly the Eflite Stearman on a few of the 4 Horsemen packs. I had stored these at 4v by accident for over a year, recharging was too fast, I figured they would be weak. I was in a rush to meet Jon, so I just packed them up. At the field I found them under-powered,but one was close. I stupidly took the Stearman up, and she flew weakly, landed a bit roughly (just a bounce), but I decided having gotten away with it I wouldn't fly the other packs. When I got home I ran them down to 3.7 V and will see if they recover.Thursday, September 3, 2020
450's are UP again!
Finished up the 450's today, the Flybarred and the Flybarless (FBL) today?
Monday, August 31, 2020
Daddy's got his Mojo back!
All good! Tomorrow I will see if the returned 10cc engine will run in the Spitty. Once that's assured, I want to fly a few more times on the iX12, though I confident with it, before maidening the Spitfire. Given my past history with Spitfires I want no doubts.
Sunday, August 30, 2020
Brain said "ABORT!", thumbs said, "WE GOT THIS!"
And that folks, is why we should not fly with our thumbs, but rather with our brains. This happened a couple of days ago, and I didn't want to revisit it...
Big 18x10 prop on an 26cc, its got some kinda torque roll. She had a bit of torque roll with the 17x8 I had on her, so no surprise this would be worse. Started the take off roll and she needed left rudder, then a little left aileron, then she needed more, than started to fly and rolled left, backed off power, Brain said, "ABORT!", but the Thumbs said, "WE GOT THIS! POWER!", she lifted more and rolled more, off the runway at 1 foot AGL and her right wing struck the high weeds, she tumbled in on to her nose. I was stunned and mad at myself! So pissed I forgot to take a photo of the crime scene, so the first pic is after pulling her out of the weeds and setting her on the runway.
Tuesday, August 25, 2020
Waco Adjustments
Last flights with the Phoenix Waco RCGF-USA 26cc, I noticed the need for a LOT of right up aileron to correct a left roll. Back in the workshop it was apparent that the left wing, which is the one I remove for transport, had a small neg deflection in the leading edge of the upper wing. I corrected this with a shim and a re-drill of the alignment peg hole inboard and installed a small shim on the outboard side. This gave her a good incidence which I think will alleviate the problem. We'll see next time I take her out.

